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Activity Name:

Levee Challenge 2021 - Team TU Delft - Use of Tyvek waterproof, damp open material and gripple anchors

Activity Numbre:

93

Activity type

Exercise

Involved Workpackage

Flood defences
Emergency response
Knowledge infrastructure

Objective

The Levee Challenge was a physical challenge in which groups of students were asked to repair the outer slope of a damaged grass covered levee against overflow.

Activity Brief descriptor

The Levee Challenge was a physical challenge in which groups of students were asked to repair the outer slope of a damaged grass covered levee.

Linked to theme(s):

Breaching
Animal- & vegetation-induced anomalies
Erosion processes
Temporary levee repairs
Levee survey & monitoring technique
Prolonged collaboration

Activity Time

Start Date:

Feb. 24, 2021, 8 a.m.

End Date:

Feb. 26, 2021, 5 p.m.

Active time length:

Days:

3

Hours:

None

Other:

The damage had to be repaired within a time frame of 4 hours. Testing happened in the following days.

Location

Levee stretch:

IV

Coordinates/ Latitude (WGS):

51.341954

Coordinates/ Longitude (WGS):

4.23771

Coordinates/ Altitude (mTAW):

None

Descriptor:

Test section on Belgian Levee. The slope is assumed to be 1:3.

Other references:

Data

Data: 1

Data type: Powerpoint, video, report
Description: Overview of testing and report
Date availability: Sept. 1, 2022
Find at:
Media avaliable: Promotional video
Find media: Promotional video

Data: 2

Data type: media
Description:
Date availability: None
Media avaliable:
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Data: 3

Data type: Report
Description:
Date availability: None
Media avaliable:
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Detaled information about the activity

Pre-conditions

Lower part of the levee was damaged by heavy traffic. Prior to the tests, 2 spots on the levee were damaged to make repairs. At the upper part of the levee slope, a cliff was dug with a width of ~1.5 m (parallel to levee slope) and a depth of 0.5-1m (deep enough to penetrate the upper clay layer).

Activity Descriptor

08:45 –09:15||30 minoverflow test at 350 l/s. 09:15 –09:20 ||5 min rest to inspect the repair solution and rest of the dike surface. 09:20 –09:50||30 min overflow test at500 l/s. 09:50 –09:20 ||5 min rest to inspect the repair solution and rest of the dikesurface. 09:55 –10:25||30 min 600 overflow test at l/s. 10:25 –10:30 ||5 min rest to inspect the repair solution and rest of the dike surface. 10:30 –11:00||30 min overflow test at 700/740 l/s. 11:00 –11:10 ||10 min rest to inspect the repair solution and rest of the dikesurface and make tear of 1 m into lower repair area (at location where water exactly hits the sheet at the bottom). 11:10 –11:40||30 min overflow test at350 l/s. 11:40 –11:45 ||5 min rest to inspect the repair solution and rest of the dike surface. 11:45 –12:45||60min overflow test at700/740 l/s.

Equipments

Equipment: 1

BA300 pump
Overflow generator

Monitoring & Sensors

this activity does not have sensors

Limits

During Activity

See Report for more information and pictures. Tests without cuts in plastic sheet - During all test volumes the plastic sheets were kept in place due to the anchors and pins. - Some of the pins (only at the bottom/toe side of some layers) came loose due to vibration of the sheets (we presume the cause of vibration is flow of water between two sheets or turbulence of water). - The grass between the two damages was flattened by the current, a typical image for overflow tests. The grass remained in place, grass clumps with roots were not pulled loose by the current. - The trench of the lower damage was partly washed away by the water. This was to be expected as the grass layer could not be kept intact when the plastic sheet was dug in. The erosion of soil in the trench did not result in changing the stability of the top sheet. The function of the buried sheet therefore remained intact. Test with cuts in plastic sheet - The lower repair failed due to high impact of water exactly on the tear. Test was done for 30 min with 350 l/swater. The tear was made through both overlapping sheet layers. - The higher repair sustained all the test also with the tear. Both tears were around 1m in the middle of the test area. The tear was only made in the upper sheet of the overlapping sheets. The soil below the upper damage was not damaged further due to the overflow tests, as could be seen after removing the repair solution. - The grass between the two damages was flattened by the current, a typical image for overflow tests. The grass remained in place, grass clumps with roots were not pulled loose by the current. So, there was no change visible between the tests with and without the cuts in the plastic sheet.

Post-activity conditions

Immediate Results

After presenting the results and improvement points, a few points of discussion remain. First, an unexpected problem was the vibrating of the plasticsheets that resulted in the extraction of the pins. It's uncertain what the long-term effect of this phenomena is, but the process may likely give positive feedback and result in a large amount of deflection. If the sheet is not tight on the dike anymore, water will flow under it resulting in erosion. Further research into mitigating this effect will be necessary. This could simply include installing more pins or trying out different straight pins to reduce the free margin around the installationpoint. A second point of concern is the proposed use of a 3 meter wide plasticsheet. Although this will reduce installation costs and time significantly, applying this sheet size under storm conditions is likely problematic. This can be best tested out by waterboard personnel in a storm situation to see the actual effects. Third, the effects of installation errors at the head of a plastic sheetsection are not yet known enough. Some initial damage was seen at the head of the bottom section, but did not propagate. Although it is unlikely that water will flow under the sheet immediately because of its curved vertical installation, it remains a critical point. What happens during installationif the soil layer is very weak after digging? Installing another sheet over the head might be a solution, but this will need to be tested further to give a reliable advice. Fourth, a large part of the anchors remains in the dike, irrespective of the proposed solution in section 6c. Although we believe this problem to be inferior with respect to the reliability and installation time during a calamity at which human lives are at stake, it remains a drawback of the solution. A final consideration is the difference in material between our used Polytex®, a Tyvek®substitute. Although Polytex®has much lower costs, the UV resistance and quality of Tyvek®might be beneficial when storing and installing the solution for prolonged periods. More research on the material qualities can contribute to the actual reliability.

Results /Conclusion

Concluding, the presented Tyvek design is an interesting solution that may well be a good contribution to the future flood protection arsenal of waterboards and other governments. The benefits related to low production costs, easy installation, and reliable storage and scaling make this innovative solution a possible advancement from classical flood protection measures, like sandbags. Further research is advised to analyse and mitigate the presented weaker spots and drawbacks.

Infrastructure Knowledge

Other key information